Merge Upstream's stable 3.0.21 branch into msm-3.0
This consists 814 commits and some merge conflicts.
The merge conflicts are because of some local changes to
msm-3.0 as well as some conflicts between google's tree and
the upstream tree.
Conflicts:
arch/arm/kernel/head.S
drivers/bluetooth/ath3k.c
drivers/bluetooth/btusb.c
drivers/mmc/core/core.c
drivers/tty/serial/serial_core.c
drivers/usb/host/ehci-hub.c
drivers/usb/serial/qcserial.c
fs/namespace.c
fs/proc/base.c
Change-Id: I62e2edbe213f84915e27f8cd6e4f6ce23db22a21
Signed-off-by: Rohit Vaswani <rvaswani@codeaurora.org>
Currently writing 0x0 into AHBMODE register which means both data
transactions and QH and TD descriptors are non-posted writes to
system memory. As per HW team recommendation, should write 0x08 value
to set AHB HPROT mode into the AHBMODE register which allows posted
data writes to system memory and will improve the throughput numbers.
Change-Id: Ib44a8cfe11c6ff96ff712643227532e24548e706
Signed-off-by: Vijayavardhan Vennapusa <vvreddy@codeaurora.org>
Clean up some error paths and simplify the code by
moving to devm_regulator_get().
Change-Id: Ifce28d4c2dfe0ed180433736ac9c815259f5359d
Signed-off-by: Mayank Rana <mrana@codeaurora.org>
A disabled IRQ that is configured as a wakeup interrupt will trigger
a system resume, however since it is disabled, its handler will never
get called and its status register is never cleared. Thus upon
subsequent suspends it causes the system to immediately resume.
This was happening in the EHCI HSIC controller, in which remote wakeup
signaling on the STROBE line is treated as a wakeup IRQ. After the
first successful wakeup sequence, when the HSIC bus goes back into low
power mode the lingering uncleared interrupt prevents a system suspend
from executing successfully. This is fixed by enabling the IRQ in the
system suspend_noirq callback. The IRQ is subsequently disabled in
either the IRQ handler or the resume callback, whichever occurs first.
CRs-fixed: 343414
Change-Id: Ifc1c267408e76b98b8d848abde6eb44df9e0cdc0
Signed-off-by: Jack Pham <jackp@codeaurora.org>
Clean up some error paths and simplify the code by
moving to devm_regulator_get().
Change-Id: I00782fd15f505002a044efadb8abdcd4adda6cc6
Signed-off-by: Mayank Rana <mrana@codeaurora.org>
With remote wakeup, usb peripheral can wakeup usb host using
resume signalling when usb bus is suspended. During XO shutdown
remote wakeup is over strobe line which is wakeup capable.
Register for strobe wakeup gpio while suspending usb hsic
controller to support remote wakeup.
Change-Id: Ia8b4d5371dbd0bdbbc86a77cc6236ae9b562a3f2
Signed-off-by: Vamsi Krishna <vskrishn@codeaurora.org>
This patch changes OTG driver to support different
OTG statemachine states for OTG2.0 complaince. It will
also enable to swap Host role between two OTG devices
via HNP and enable B device to request A device to start
VBUS session via SRP.
Change-Id: Ibe2519ff1570768f51e879af483a6f5c23b38d8f
Signed-off-by: Vijayavardhan Vennapusa <vvreddy@codeaurora.org>
Signed-off-by: Pavankumar Kondeti <pkondeti@codeaurora.org>
EHCI core intiates HNP by calling otg_start_hnp() API when OTG port
is put into suspend to notify OTG driver which will take care of
HNP by suspending host and kicking gadget.
Change-Id: I2982b9f49140c2dcf2a32691e74f177e8d5d08cb
Signed-off-by: Vijayavardhan Vennapusa <vvreddy@codeaurora.org>
Liquid platform on 8064 has ehci compliant HSUSB core4 to support
GOBI module via PCIe MINI Card CONNECTOR. This patch adds platform
device instance for EHCI compliant USB Host Controller driver.
Change-Id: I0d01babc3a818b308216bb57e48522cd2b62e07c
Signed-off-by: Hemant Kumar <hemantk@codeaurora.org>
Currently, ehci driver votes for VDD minimization when USB bus goes
to suspend. PHY will not generate interrupt if driver votes for VDD
minimization. Hence set the VDDCX suspend voltage to 0.75V when Liquid
is attached to docking station, so that phy can generate interrupt
as a result of a device plug in.
Change-Id: Iab0bc2855e7729f30ca5665014670e8fa6ca313d
Signed-off-by: Hemant Kumar <hemantk@codeaurora.org>
This change implements the docking station detection by reading the status
of MPP9 on PMIC8921. With this change VREG_5V(USB port 3 VBUS) is turned on
only when docking station is connected to Liquid platform in order to save
power.
Change-Id: I4282b4273adabf8aeaf8faad43cd2cfff36eeac6
Signed-off-by: Hemant Kumar <hemantk@codeaurora.org>
This patch adds support for EHCI compliant USB Host Controller
for Liquid on 8064.
This driver supports Host only mode and is different from ehci-msm
which relies on OTG driver for putting hardware in low pwer mode
and PHY initialization as well.
Change-Id: I84b63b2577311900a0b434f53df547bad62f6316
Signed-off-by: Manu Gautam <mgautam@codeaurora.org>
Signed-off-by: Hemant Kumar <hemantk@codeaurora.org>
The HSIC controller may be in suspend state in which its clocks
are already disabled. Fix warning given by clock subsystem when
disabling the clocks a second time when the controller's platform
device is removed by first checking if the device is suspended.
Change-Id: Id6e6f01673b93a48de5e36afe3de44a5a4dc632e
Signed-off-by: Jack Pham <jackp@codeaurora.org>
When the HSIC peripheral is disconnected, its platform device is
removed via platform_device_del(), which increments the PM
disable_depth counter. The EHCI driver's remove callback is
additionally calling pm_runtime_disable() which increments the
counter again. When the peripheral is reconnected via
platform_device_add() only the probe callback is calling
pm_runtime_enable() which leads to an unbalanced counter.
Change-Id: I28bcd20568d93a48c760551b701a234edaec5ecc
Signed-off-by: Jack Pham <jackp@codeaurora.org>
To add support for 9615, the following changes were made in the host file:
1. Add HSIC host initialization for non-GPIO configuration.
2. Add support for no-pdata (which is not needed for
non-GPIO configuration)
3. Move set_clk_rate calls to target specific clock files.
Change-Id: Icecd65d0b8467a4e4b1696ff0e14aa759d1be679
Signed-off-by: Lena Salman <esalman@codeaurora.org>
Clock framework now provides two new APIs: clk_prepare and
clk_unprepare which can be called from non-atomic context only.
Other clk_enable and clk_disable APIs can be called from atomic
context.
To enable a clock drivers need to call both clk_prepare and
clk_enable. Similarly for disabling a clock - clk_disable and
clk_unprepare should be called.
Change-Id: I1ec0764e34619b92d811e1dadd2bb49b5cf36f5c
Signed-off-by: Manu Gautam <mgautam@codeaurora.org>
commit e4436a7c17ac2b5e138f93f83a541cba9b311685 upstream.
The Netlogic XLP SoC's on-chip USB controller appears as a PCI
USB device, but does not need the EHCI/OHCI handoff done in
usb/host/pci-quirks.c.
The pci-quirks.c is enabled for all vendors and devices, and is
enabled if USB and PCI are configured.
If we do not skip the qurik handling on XLP, the readb() call in
ehci_bios_handoff() will cause a crash since byte access is not
supported for EHCI registers in XLP.
Signed-off-by: Jayachandran C <jayachandranc@netlogicmicro.com>
Acked-by: Alan Stern <stern@rowland.harvard.edu>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit cf840551a884360841bd3d3ce1ad0868ff0b759a upstream.
When a TD length mismatch is found during isoc TRB enqueue, it directly
returns -EINVAL. However, isoc transfer is partially enqueued at this time,
and the ring should be cleared.
This should be backported to kernels as old as 2.6.36, which contain the
commit 522989a27c7badb608155b1f1dea3487ed431f74 "xhci: Fix failed
enqueue in the middle of isoch TD."
Signed-off-by: Andiry Xu <andiry.xu@amd.com>
Signed-off-by: Sarah Sharp <sarah.a.sharp@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit d0cd5d482b8a6dc92c6c69a5387baf72ea84f23a upstream.
The xHCI hub port code gets passed a zero-based port number by the USB
core. It then adds one to in order to find a device slot by port number
and device speed by calling xhci_find_slot_id_by_port. That function
clearly states it requires a one-based port number. The xHCI port
status change event handler was using a zero-based port number that it
got from find_faked_portnum_from_hw_portnum, not a one-based port
number. This lead to the doorbells never being rung for a device after
a resume, or worse, a different device with the same speed having its
doorbell rung (which could lead to bad power management in the xHCI host
controller).
This patch should be backported to kernels as old as 2.6.39.
Signed-off-by: Sarah Sharp <sarah.a.sharp@linux.intel.com>
Acked-by: Andiry Xu <andiry.xu@amd.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit 2492c6e6454ff3edb11e273b071a6ea80a199c71 upstream.
Add missing iounmap in error handling code, in a case where the function
already preforms iounmap on some other execution path.
A simplified version of the semantic match that finds this problem is as
follows: (http://coccinelle.lip6.fr/)
// <smpl>
@@
expression e;
statement S,S1;
int ret;
@@
e = \(ioremap\|ioremap_nocache\)(...)
... when != iounmap(e)
if (<+...e...+>) S
... when any
when != iounmap(e)
*if (...)
{ ... when != iounmap(e)
return ...; }
... when any
iounmap(e);
// </smpl>
Signed-off-by: Julia Lawall <Julia.Lawall@lip6.fr>
Acked-by: Alan Stern <stern@rowland.harvard.edu>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
commit c61875977458637226ab093a35d200f2d5789787 upstream.
Problems with NVIDIA's OHCI host controllers persist. After looking
carefully through the spec, I finally realized that when a controller
is reset it then automatically goes into a SUSPEND state in which it
is completely quiescent (no DMA and no IRQs) and from which it will
not awaken until the system puts it into the OPERATIONAL state.
Therefore there's no need to worry about controllers being in the
RESET state for extended periods, or remaining in the OPERATIONAL
state during system shutdown. The proper action for device
initialization is to put the controller into the RESET state (if it's
not there already) and then to issue a software reset. Similarly, the
proper action for device shutdown is simply to do a software reset.
This patch (as1499) implements such an approach. It simplifies
initialization and shutdown, and allows the NVIDIA shutdown-quirk code
to be removed.
Signed-off-by: Alan Stern <stern@rowland.harvard.edu>
Tested-by: Andre "Osku" Schmidt <andre.osku.schmidt@googlemail.com>
Tested-by: Arno Augustin <Arno.Augustin@web.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit 18b7ede5f7ee2092aedcb578d3ac30bd5d4fc23c upstream.
[ removed the dwc3 portion of the patch as it didn't apply to
older kernels - gregkh]
According to USB 3.0 Specification Table 9-22, if
bmAttributes [4:0] are set to zero, it means "no
streams supported", but the way this helper was
defined on Linux, we will *always* have one stream
which might cause several problems.
For example on DWC3, we would tell the controller
endpoint has streams enabled and yet start transfers
with Stream ID set to 0, which would goof up the host
side.
While doing that, convert the macro to an inline
function due to the different checks we now need.
Signed-off-by: Felipe Balbi <balbi@ti.com>
Signed-off-by: Sarah Sharp <sarah.a.sharp@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit 71d85724bdd947a3b42a88d08af79f290a1a767b upstream.
I encountered a result of COMP_2ND_BW_ERR while improving how the pwc
webcam driver handles not having the full usb1 bandwidth available to
itself.
I created the following test setup, a NEC xhci controller with a
single TT USB 2 hub plugged into it, with a usb keyboard and a pwc webcam
plugged into the usb2 hub. This caused the following to show up in dmesg
when trying to stream from the pwc camera at its highest alt setting:
xhci_hcd 0000:01:00.0: ERROR: unexpected command completion code 0x23.
usb 6-2.1: Not enough bandwidth for altsetting 9
And usb_set_interface returned -EINVAL, which caused my pwc code to not
do the right thing as it expected -ENOSPC.
This patch makes the xhci driver properly handle COMP_2ND_BW_ERR and makes
usb_set_interface return -ENOSPC as expected.
This should be backported to stable kernels as old as 2.6.32.
Signed-off-by: Hans de Goede <hdegoede@redhat.com>
Signed-off-by: Sarah Sharp <sarah.a.sharp@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit bc677d5b64644c399cd3db6a905453e611f402ab upstream.
Add a new field num_mapped_sgs to struct urb so that we have a place to
store the number of mapped entries and can also retain the original
value of entries in num_sgs. Previously, usb_hcd_map_urb_for_dma()
would overwrite this with the number of mapped entries, which would
break dma_unmap_sg() because it requires the original number of entries.
This fixes warnings like the following when using USB storage devices:
------------[ cut here ]------------
WARNING: at lib/dma-debug.c:902 check_unmap+0x4e4/0x695()
ehci_hcd 0000:00:12.2: DMA-API: device driver frees DMA sg list with different entry count [map count=4] [unmap count=1]
Modules linked in: ohci_hcd ehci_hcd
Pid: 0, comm: kworker/0:1 Not tainted 3.2.0-rc2+ #319
Call Trace:
<IRQ> [<ffffffff81036d3b>] warn_slowpath_common+0x80/0x98
[<ffffffff81036de7>] warn_slowpath_fmt+0x41/0x43
[<ffffffff811fa5ae>] check_unmap+0x4e4/0x695
[<ffffffff8105e92c>] ? trace_hardirqs_off+0xd/0xf
[<ffffffff8147208b>] ? _raw_spin_unlock_irqrestore+0x33/0x50
[<ffffffff811fa84a>] debug_dma_unmap_sg+0xeb/0x117
[<ffffffff8137b02f>] usb_hcd_unmap_urb_for_dma+0x71/0x188
[<ffffffff8137b166>] unmap_urb_for_dma+0x20/0x22
[<ffffffff8137b1c5>] usb_hcd_giveback_urb+0x5d/0xc0
[<ffffffffa0000d02>] ehci_urb_done+0xf7/0x10c [ehci_hcd]
[<ffffffffa0001140>] qh_completions+0x429/0x4bd [ehci_hcd]
[<ffffffffa000340a>] ehci_work+0x95/0x9c0 [ehci_hcd]
...
---[ end trace f29ac88a5a48c580 ]---
Mapped at:
[<ffffffff811faac4>] debug_dma_map_sg+0x45/0x139
[<ffffffff8137bc0b>] usb_hcd_map_urb_for_dma+0x22e/0x478
[<ffffffff8137c494>] usb_hcd_submit_urb+0x63f/0x6fa
[<ffffffff8137d01c>] usb_submit_urb+0x2c7/0x2de
[<ffffffff8137dcd4>] usb_sg_wait+0x55/0x161
Signed-off-by: Clemens Ladisch <clemens@ladisch.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Drivers should now use their device names to distinguish between
clocks of the same type rather than the clock name. Clock names
are updated to match the new naming convention.
CRs-Fixed: 327559
Change-Id: I78757806589e037a0655a63e7ee20c935214c99d
Signed-off-by: Manu Gautam <mgautam@codeaurora.org>
External modem is connected to Apps processor over HSIC interface.
This interface is used in boot loader for image download and in
HLOS for Rmnet, DUN, DIAG etc. After image download, during ext
modem HLOS boot-up, resets the HSIC controller and goes into
discovery phase.
On Apps processor, HSIC can put strobe/data into IDLE state because
of bus suspend. At this point, if external modem resets the HSIC
h/w and goes into discovery and connect phase as HSIC bus is in IDLE.
As Apps processor is not in discovery state, may miss the connect
event which can lead to enumeration failure. To avoid such issues,
put HSIC lines into reset on external modem status change event.
Change-Id: I9df163da2d8dbfb2a12b75c4485379886fa47174
Signed-off-by: Vamsi Krishna <vskrishn@codeaurora.org>
Signed-off-by: Ramakrishna Prasad N <crpn@codeaurora.org>
commit 158886cd2cf4599e04f9b7e10cb767f5f39b14f1 upstream.
When system enters suspend, xHCI driver clears command ring by writing zero
to all the TRBs. However, this also writes zero to the Link TRB, and the ring
is mangled. This may cause driver accesses wrong memory address and the
result is unpredicted.
When clear the command ring, keep the last Link TRB intact, only clear its
cycle bit. This should fix the "command ring full" issue reported by Oliver
Neukum.
This should be backported to stable kernels as old as 2.6.37, since the
commit 89821320 "xhci: Fix command ring replay after resume" is merged.
Signed-off-by: Andiry Xu <andiry.xu@amd.com>
Signed-off-by: Sarah Sharp <sarah.a.sharp@linux.intel.com>
Reported-by: Oliver Neukum <oneukum@suse.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit e3420901eba65b1c46bed86d360e3a8685d20734 upstream.
Fix a regression that was introduced by commit
811c926c538f7e8d3c08b630dd5844efd7e000f6 (USB: EHCI: fix HUB TT scheduling
issue with iso transfer).
We detect an error if next == start, but this means uframe 0 can't be allocated
anymore for iso transfer...
Reported-by: Sander Eikelenboom <linux@eikelenboom.it>
Signed-off-by: Matthieu CASTET <castet.matthieu@free.fr>
Acked-by: Alan Stern <stern@rowland.harvard.edu>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit 811c926c538f7e8d3c08b630dd5844efd7e000f6 upstream.
The current TT scheduling doesn't allow to play and then record on a
full-speed device connected to a high speed hub.
The IN iso stream can only start on the first uframe (0-2 for a 165 us)
because of CSPLIT transactions.
For the OUT iso stream there no such restriction. uframe 0-5 are possible.
The idea of this patch is that the first uframe are precious (for IN TT iso
stream) and we should allocate the last uframes first if possible.
For that we reverse the order of uframe allocation (last uframe first).
Here an example :
hid interrupt stream
----------------------------------------------------------------------
uframe | 0 | 1 | 2 | 3 | 4 | 5 | 6 | 7 |
----------------------------------------------------------------------
max_tt_usecs | 125 | 125 | 125 | 125 | 125 | 125 | 30 | 0 |
----------------------------------------------------------------------
used usecs on a frame | 13 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
----------------------------------------------------------------------
iso OUT stream
----------------------------------------------------------------------
uframe | 0 | 1 | 2 | 3 | 4 | 5 | 6 | 7 |
----------------------------------------------------------------------
max_tt_usecs | 125 | 125 | 125 | 125 | 125 | 125 | 30 | 0 |
----------------------------------------------------------------------
used usecs on a frame | 13 | 125 | 39 | 0 | 0 | 0 | 0 | 0 |
----------------------------------------------------------------------
There no place for iso IN stream (uframe 0-2 are used) and we got "cannot
submit datapipe for urb 0, error -28: not enough bandwidth" error.
With the patch this become.
iso OUT stream
----------------------------------------------------------------------
uframe | 0 | 1 | 2 | 3 | 4 | 5 | 6 | 7 |
----------------------------------------------------------------------
max_tt_usecs | 125 | 125 | 125 | 125 | 125 | 125 | 30 | 0 |
----------------------------------------------------------------------
used usecs on a frame | 13 | 0 | 0 | 0 | 125 | 39 | 0 | 0 |
----------------------------------------------------------------------
iso IN stream
----------------------------------------------------------------------
uframe | 0 | 1 | 2 | 3 | 4 | 5 | 6 | 7 |
----------------------------------------------------------------------
max_tt_usecs | 125 | 125 | 125 | 125 | 125 | 125 | 30 | 0 |
----------------------------------------------------------------------
used usecs on a frame | 13 | 0 | 125 | 40 | 125 | 39 | 0 | 0 |
----------------------------------------------------------------------
Signed-off-by: Matthieu Castet <matthieu.castet@parrot.com>
Signed-off-by: Thomas Poussevin <thomas.poussevin@parrot.com>
Signed-off-by: Alan Stern <stern@rowland.harvard.edu>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit 8746c83d538cab273d335acb2be226d096f4a5af upstream.
qset->qh.link is an __le64 field and we should be using cpu_to_le64()
to fill it.
Signed-off-by: Dan Carpenter <dan.carpenter@oracle.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit 811c926c538f7e8d3c08b630dd5844efd7e000f6 upstream.
The current TT scheduling doesn't allow to play and then record on a
full-speed device connected to a high speed hub.
The IN iso stream can only start on the first uframe (0-2 for a 165 us)
because of CSPLIT transactions.
For the OUT iso stream there no such restriction. uframe 0-5 are possible.
The idea of this patch is that the first uframe are precious (for IN TT iso
stream) and we should allocate the last uframes first if possible.
For that we reverse the order of uframe allocation (last uframe first).
Here an example :
hid interrupt stream
----------------------------------------------------------------------
uframe | 0 | 1 | 2 | 3 | 4 | 5 | 6 | 7 |
----------------------------------------------------------------------
max_tt_usecs | 125 | 125 | 125 | 125 | 125 | 125 | 30 | 0 |
----------------------------------------------------------------------
used usecs on a frame | 13 | 0 | 0 | 0 | 0 | 0 | 0 | 0 |
----------------------------------------------------------------------
iso OUT stream
----------------------------------------------------------------------
uframe | 0 | 1 | 2 | 3 | 4 | 5 | 6 | 7 |
----------------------------------------------------------------------
max_tt_usecs | 125 | 125 | 125 | 125 | 125 | 125 | 30 | 0 |
----------------------------------------------------------------------
used usecs on a frame | 13 | 125 | 39 | 0 | 0 | 0 | 0 | 0 |
----------------------------------------------------------------------
There no place for iso IN stream (uframe 0-2 are used) and we got "cannot
submit datapipe for urb 0, error -28: not enough bandwidth" error.
With the patch this become.
iso OUT stream
----------------------------------------------------------------------
uframe | 0 | 1 | 2 | 3 | 4 | 5 | 6 | 7 |
----------------------------------------------------------------------
max_tt_usecs | 125 | 125 | 125 | 125 | 125 | 125 | 30 | 0 |
----------------------------------------------------------------------
used usecs on a frame | 13 | 0 | 0 | 0 | 125 | 39 | 0 | 0 |
----------------------------------------------------------------------
iso IN stream
----------------------------------------------------------------------
uframe | 0 | 1 | 2 | 3 | 4 | 5 | 6 | 7 |
----------------------------------------------------------------------
max_tt_usecs | 125 | 125 | 125 | 125 | 125 | 125 | 30 | 0 |
----------------------------------------------------------------------
used usecs on a frame | 13 | 0 | 125 | 40 | 125 | 39 | 0 | 0 |
----------------------------------------------------------------------
Signed-off-by: Matthieu Castet <matthieu.castet@parrot.com>
Signed-off-by: Thomas Poussevin <thomas.poussevin@parrot.com>
Signed-off-by: Alan Stern <stern@rowland.harvard.edu>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit 97ff22ee3b4cb3a334f7385e269773141aed702f upstream.
This patch (as1491) works around a bug in GCC-3.4.6, which is still
supposed to be supported. The number of microseconds in the udelay()
call in quirk_usb_disable_ehci() is fixed at 100, but the compiler
doesn't understand this and generates a link-time error. So we
replace the otherwise unused variable "delta" with a simple constant
100. This same pattern is already used in other delay loops in that
source file.
Signed-off-by: Alan Stern <stern@rowland.harvard.edu>
Reported-by: Konrad Rzepecki <krzepecki@dentonet.pl>
Tested-by: Konrad Rzepecki <krzepecki@dentonet.pl>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit f69e3120df82391a0ee8118e0a156239a06b2afb upstream.
This patch (as1494) fixes a problem in xhci-hcd's resume routine.
When the controller is runtime-resumed, this can only mean that one of
the two root hubs has made a wakeup request and therefore needs to be
resumed as well. Rather than try to determine which root hub requires
attention (which might be difficult in the case where a new
non-SuperSpeed device has been plugged in), the patch simply resumes
both root hubs.
Without this change, there is a race: The controller might be put back
to sleep before it can activate its IRQ line, and the wakeup condition
might never get handled.
The patch also simplifies the logic in xhci_resume a little, combining
some repeated flag settings into a single pair of statements.
Signed-off-by: Alan Stern <stern@rowland.harvard.edu>
CC: Sarah Sharp <sarah.a.sharp@linux.intel.com>
Tested-by: Linus Torvalds <torvalds@linux-foundation.org>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
* common/android-3.0: (570 commits)
misc: remove kernel debugger core
ARM: common: fiq_debugger: dump sysrq directly to console if enabled
ARM: common: fiq_debugger: add irq context debug functions
net: wireless: bcmdhd: Call init_ioctl() only if was started properly for WEXT
net: wireless: bcmdhd: Call init_ioctl() only if was started properly
net: wireless: bcmdhd: Fix possible memory leak in escan/iscan
cpufreq: interactive governor: default 20ms timer
cpufreq: interactive governor: go to intermediate hi speed before max
cpufreq: interactive governor: scale to max only if at min speed
cpufreq: interactive governor: apply intermediate load on current speed
ARM: idle: update idle ticks before call idle end notifier
input: gpio_input: don't print debounce message unless flag is set
net: wireless: bcm4329: Skip dhd_bus_stop() if bus is already down
net: wireless: bcmdhd: Skip dhd_bus_stop() if bus is already down
net: wireless: bcmdhd: Improve suspend/resume processing
net: wireless: bcmdhd: Check if FW is Ok for internal FW call
tcp: Don't nuke connections for the wrong protocol
ARM: common: fiq_debugger: make uart irq be no_suspend
net: wireless: Skip connect warning for CONFIG_CFG80211_ALLOW_RECONNECT
mm: avoid livelock on !__GFP_FS allocations
...
Conflicts:
arch/arm/mm/cache-l2x0.c
arch/arm/vfp/vfpmodule.c
drivers/mmc/core/host.c
kernel/power/wakelock.c
net/bluetooth/hci_event.c
Signed-off-by: Bryan Huntsman <bryanh@codeaurora.org>
In current design, PM usage counter operations are scattered across
charging detection work, state machine work, interrupt handler and
resume work. This did not give any problems for typical device mode
or host mode use cases. But with ACA implementation, there will be
many corner cases where PM usage operations can go wrong and device
stays out of low power mode (LPM). Hence leave PM usage counter
operations to state machine work, which knows best about the device
state.
Don't create device and host controller platform devices as children
of OTG device. This helps OTG state machine to know about host bus
suspend and can take a decision whether low power mode is possible or
not.
Change-Id: I00474e396546d2567d09409e70591a6c9d325c06
Signed-off-by: Pavankumar Kondeti <pkondeti@codeaurora.org>
At times, USB PHY suspend fails and keeps it vote for higher VDDCx
resulting in high power numbers. Hence request for lower VDDCx, even
if phy suspend fails.
Change-Id: Iba79f93641a665c7f681af02c4dbe59cacddd18a
Signed-off-by: Chiranjeevi Velempati <cvelempa@codeaurora.org>
commit 6fd4562178508a0949c9fdecd8558d8b10d671bd upstream.
When the link state changes, xHC will report a port status change event
and set the PORT_PLC bit, for both USB3 and USB2 root hub ports.
The PLC will be cleared by usbcore for USB3 root hub ports, but not for
USB2 ports, because they do not report USB_PORT_STAT_C_LINK_STATE in
wPortChange.
Clear it for USB2 root hub ports in handle_port_status().
Signed-off-by: Andiry Xu <andiry.xu@amd.com>
Signed-off-by: Sarah Sharp <sarah.a.sharp@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit 2dc3753997f3c80ce8b950242ab9bb3fb936acfd upstream.
Some alternate interface settings have no endpoints associated with them.
This shows up in some USB webcams, particularly the Logitech HD 1080p,
which uses the uvcvideo driver. If a driver switches between two alt
settings with no endpoints, there is no need to issue a configure endpoint
command, because there is no endpoint information to update.
The only time a configure endpoint command with just the add slot flag set
makes sense is when the driver is updating hub characteristics in the slot
context. However, that code never calls xhci_check_bandwidth, so we
should be safe not issuing a command if only the slot context add flag is
set.
Signed-off-by: Sarah Sharp <sarah.a.sharp@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit c2d7b49f42f50d7fc5cbfd195b785a128723fdf4 upstream.
When a xHC host is unable to handle isochronous transfer in the
interval, it reports a Missed Service Error event and skips some tds.
Currently xhci driver handles MSE event in the following ways:
1. When encounter a MSE event, set ep->skip flag, update event ring
dequeue pointer and return.
2. When encounter the next event on this ep, the driver will run the
do-while loop, fetch td from ep's td_list to find the td
corresponding to this event. All tds missed are marked as short
transfer(-EXDEV).
The do-while loop will end in two ways:
1. If the td pointed by the event trb is found;
2. If the ep ring's td_list is empty.
However, if a buggy HW reports some unpredicted event (for example, an
overrun event following a MSE event while the ep ring is actually not
empty), the driver will never find the td, and it will loop until the
td_list is empty.
Unfortunately, the spinlock is dropped when give back a urb in the
do-while loop. During the spinlock released period, the class driver
may still submit urbs and add tds to the td_list. This may cause
disaster, since the td_list will never be empty and the loop never ends,
and the system hangs.
To fix this, count the number of TDs on the ep ring before skipping TDs,
and quit the loop when skipped that number of tds. This guarantees the
do-while loop will end after certain number of cycles, and driver will
not be trapped in an infinite loop.
Signed-off-by: Andiry Xu <andiry.xu@amd.com>
Signed-off-by: Sarah Sharp <sarah.a.sharp@linux.intel.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
commit 77636c86a600b83de01719efad83567e46d7e8ce upstream.
The sequence to put port in test mode is not complete.
According EHCI specification all enabled ports must be
put in suspend.
Signed-off-by: Boris Todorov <boris.st.todorov@gmail.com>
Acked-by: Alan Stern <stern@rowland.harvard.edu>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit 273d23574f9dacd9c63c80e7d63639a669aad441 upstream.
For USB CONTROL transaction, when the data length is zero,
the IN package is needed to finish this transaction in status stage.
Signed-off-by: Jerry Huang <r66093@freescale.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>
commit a8b43c00ef06aec49b9fe0a5bad8a6a320e4d27b upstream.
At least some OHCI hardware (such as the MCP89) fails to flag any change
in the host status register or the port status registers when receiving
a remote wakeup while in D3 state. This results in the controller being
resumed but no device state change being noticed, at which point the
controller is put back to sleep again. Since there doesn't seem to be any
reliable way to identify the state change, just unconditionally resume the
hub. It'll be put back to sleep in the near future anyway if there are no
active devices attached to it.
Signed-off-by: Matthew Garrett <mjg@redhat.com>
Cc: Alan Stern <stern@rowland.harvard.edu>
Signed-off-by: Greg Kroah-Hartman <gregkh@suse.de>